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SIDEBAR:
Making an Easy Fix in the Field
The GE Lighting Euclid Lamp Plant manufactures a variety of industrial, household, and automotive lamps. In the production of automotive lamps, the bulb, exhaust tube, and mount structure—consisting of lead wires and coil—are sealed together by heating the bulb and mechanically pinching the glass to form a seal around the lead wires and exhaust tube. This process results in great residual stress on the bulb. To minimize the effect, the bulb is heated above a critical temperature and then cooled in a controlled fashion to relieve the mechanical stress, improve product strength, and meet quality parameters.

GE had to monitor each lamp in a temperature range between 650°C and 950°C. High levels of signal attenuation caused by environmental factors and mechanical obstructions led GE to choose an IR ratio-thermometer with peak-hold signal conditioning. After testing the device in the lab, GE purchased a Raytek Marathon MR1S integrated ratio-thermometer. Once the unit was installed on the production line, though, things worked differently. Although the temperature values being reported were mostly correct, an occassional value would be reported that could not be explained based on the process parameters.

Guido Bergomi, quality engineer at the plant, immediately contacted Raytek in Santa Cruz, California, to notify the company of the problem. Bergomi was able to connect the sensor to a computer and record process data while the unit was online. Thomas Heinke, design engineer at Raytek, analyzed the data Bergomi provided.

"The correct temperature readings were in the raw data," says Heinke. "However, the speed of the process, the momentary blockage of the reading, and the highly attenuated signal could all combine to cause the peak-hold algorithm to trigger on an invalid signal." Based on the data from GE, Heinke was able to develop a custom peak-hold algorithm for the sensor and send a firmware upgrade. The upgrade was uploaded via two-way communications to the firmware in the Marathon MR1S's electronics.

"I thought the units would have to go back to the factory," says Bergomi. "I was surprised and pleased that the modifications to the firmware could be made in the field. I just hooked the unit to my computer and ran the program.

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